Detailed benchmarking of specific steam consumption (SSC) and condensate recovery factor (CRF) through plant survey and site assessments.
Reduction of medium pressure steam usage in coaters by:
- Improving trap uptime for all coater heaters
- Using medium pressure condensate flash in low pressure dryer groups
- Installing an On/Off control system to cut steam during paper breaks
Conversion of MG dryer TC (mechanical glazing dryer thermocompressor) system from motive steam-based to cascade-based operation, reducing medium pressure steam usage.
Changing of 25 Tonnes Per Day (55K Pounds Per Day) medium pressure steam by converting it into low pressure steam, enhancing turbine house power generation.
Continuous digital monitoring and proactive maintenance of control system uptime, including pressure loops, differential pressure control loops, level control loops, and other instrumentation.
Preparation of GSM-wise and speed-wise recipes for optimised pressure and differential pressure control loops settings to ensure lower energy consumption and improved production quality.